Date: June 2nd, 1983
Type: McDonnell Douglas DC-9-32
Registration: -
Operator: Air Canada
Where: Cincinnati-Greater Cincinnati APT (USA)
Report No.: NTSB/AAR-84/09
Report Date: -
Pages: -
This is not an accident investigation report.
At 16.25h CDT Flight 797 took off from Dallas for a flight to Montreal via
Toronto. At 18.51h EDT, while cruising at FL330, the three aft lavatory
flush motor circuit breakers tripped. The captain thought the plush motor
had probably seized and waited for about eight minutes before
(unsuccessfully) trying to reset them. At about the same time a strange
odor was smelled at the aft of the plane. After finding out that the
lavatory was full of smoke, a cabin attendant used the CO2 bottle to put
out the fire (though only black smoke was seen coming out of the seams of
the lavatotory's walls).
The first officer went over to take a look, but had to returnb to the
cockpit to get his goggles. When returning to the cockpit at 19.07h, the
1st officer told the captain he thought it best to descend. Around that
time the aircraft started developing electrical problems and a Mayday call
was issued. Flight 797 stared to descend and contacted Cincinnati at 19.10h
for an emergency. During the desent smoke began to fill the passenger
cabin. The emergency landing was carried out on Runway 27L at 19.20h. The
Cincinnati fire services were not able to put out the fire, which gutted
the fuselage.
PROBABLE CAUSE: "A fire of undetermined origin, an underestimate of fire
severity, and conflicting fire progress information provided to the
captain.
Contributing to the severity of the accident was the flightcrew's delayed
decision to institute an emergency descent." (NTSB/AAR-84/09)
Source: NTSB/AAR-84/09